ISSN:1003-8620

CN:42-1243/TF

主管:中信泰富特钢集团股份有限公司

主办:大冶特殊钢有限公司

特殊钢 ›› 2017, Vol. 38 ›› Issue (6): 23-26.

• 工艺技术 • 上一篇    下一篇

25Mn钢Φ185mmx13mm冷拔管内表面麻点状缺陷的分析和控制工艺

邓明明1,彭其春1,肖云清1,彭自胜2,肖鸿光2,范其良2   

  1. 1. 武汉科技大学钢铁冶金及资源利用省部共建教育部重点实验室,武汉430081 ;
    2. 华菱集团衡阳钢管(集团)有限公司,衡阳421001
  • 出版日期:2017-12-01 发布日期:2022-07-09
  • 作者简介:邓明明(1992-),男,硕士研究生,2015年武汉科技大学(本科)毕业,铸坯与轧材质量控制研究。

Analysis on Mottled Spots Defect of Internal Surface of Φ185mmx13mm Cold-Drawn Tube of Steel 25Mn

Deng Mingming1, Peng Qichun1, Xiao Yunqing1, Peng Zisheng2, Xiao Hongguang2, Fan Qiliang2   

  1. 1. Key Laboratory for Ferrous Metallurgy and Resources Utilization of Ministry Education, Wuhan University of Science and Technology, Wuhan 430081;
    2. Hengyang Steel Tube Co Ltd, Hualing Group, 421001
  • Published:2017-12-01 Online:2022-07-09

摘要: 25Mn钢(/%:0.24C,0.25Si,0.87Mn,0.016P,0.011S)冷拔管的生产流程为铁水预处理-90tEAF-LFVD-Φ250mm圆坯HCC-穿孔-热轧至Φ197mm×17mm管-冷拔至Φ185mm×13mm管。采用光学、扫描电子显微镜、能谱仪和电子探针分析了25Mn钢冷拔管内表面麻点状缺陷。结果表明,麻点状缺陷呈翘皮状和凹坑状,翘皮状缺陷成因是CaO-Al2O3-(MgO)复合夹杂与钢基体变形量不一,凹坑状缺陷成因是Al2O3-MnS-CaS复合夹杂聚集长大后磨削加工过程中脱落。通过将原铝脱氧精炼工艺优化成硅钙合金脱氧工艺,使精炼渣碱度由原6.76降至2.26,精炼渣中(MgO)由原5.33%提高至7.23%,(Al2O3)由26.05%降低至12.76%,使钢中的硬脆性夹杂转变为延展性优良的硅酸盐类夹杂,消除了25Mn钢冷拔管内表面麻点状缺陷。

关键词: 25Mn钢, Φ185mmx13mm冷拔管, 麻点状缺陷, 复合夹杂, 硅钙线脱氧, 精炼渣碱度

Abstract: The production flowsheet for cold-drawn tube of steel 25Mn(/%: 0.24C, 0.25Si, 0.87Mn, 0.016P, 0.011S) is hot-metal pretreatment-90t EAF-LF-VD-Φ250mm round bloom HCC-piercing-hol rolling to Φ197mmx17mm tube-cold rolling to Φ185mmx13mm tube. The mottled spots delect of internal surface of steel 25Mn cold-drawn tube is analyzed by using optical microscope, scanning electron microscope (SEM) , energy spectnam meter and electron probe analyzer. Results show that the mottled spots defect is warped skin and concave pitting;the warped skin defect is caused by aggregated CaO-Al2O3-(MgO) compound inclusions which deformation is different from base steel and the aggregated growing up of Al2O3-MnS-CaS compound inclusions fall off in cutting process to form concave pitting. With optimizing the original aluminium deoxidizing process to silico-calcium alloy deoxidizing process, decreasing the refining slag basicity from original 6.76 to 2.26, increasing the refining slag (MgO) from 5.33% to 7.23% and decreasing the ( Al2O3 ) from 26.05% to 12.76% to modify the brittle inclusions in steel to silicate inclusions with better ductility, therefore the internal mottled spots defect of internal surface of steel 25Mn cold-drawn tube is eliminated.