ISSN:1003-8620

CN:42-1243/TF

主管:中信泰富特钢集团股份有限公司

主办:大冶特殊钢有限公司

特殊钢 ›› 2015, Vol. 36 ›› Issue (6): 33-35.

• 工艺技术 • 上一篇    下一篇

超低碳钢210 t RH脱碳精炼工艺的优化

周剑丰,罗钢   

  1. 湖南华菱涟源钢铁有限公司技术中心,娄底417009
  • 收稿日期:2015-06-19 出版日期:2015-12-01 发布日期:2022-08-12
  • 作者简介:周剑丰(1977-),男,硕士(2008年武汉科技大学),工程师, 1998年贵州大学(本科)毕业,从事纯净钢冶炼研究。

Optimization of 210 t RH Decarburization Process for Ultra-Low Carbon Steel Refining

Zhou Jianfeng , Luo Gang   

  1. Technical Center, Lianyuan Iron and Steel Co Ltd, Hunan Hualing, Loudi 417009
  • Received:2015-06-19 Published:2015-12-01 Online:2022-08-12

摘要: 分析和确定了RH精炼的初始碳含量、提升气体流量和转炉终点氧含量,并进行生产实践。结果表明,RH进站初始碳含量应控制在250×10-6~400×10-6,转炉出钢时终点氧含量应控制在250×10-6~400×10-6。实际生产数据统计表明,在PH处理初期(0~3 min),各炉次脱碳速率最大值可达到98×10-6/min,在脱碳终点时,碳含量在12×10-6左右。

关键词: 210t RH, 超低碳钢, 脱碳, 工艺优化

Abstract: The RH refining initial carbon content in liquid, rising gas rate and converter end oxygen content in liquid are analyzed and defined, and the production practice has carried out. The results show that the initial carbon content in liquid before RH refining should be controlled from 250 x 10-6 to 400 x 10-6, the end oxygen content in liquid of converter at tapping should be controlled from 250 x 10-6 to 400 X 10-6. The statistic data of real production show that in beginning period of RH refining for 0 ~3 min, the max decarburization rate of each heat is up to 98 x 10-6/min, and at end of decarburization the carbon content in liquid is about 12 x 10-6.