致使大量的细小的BN在晶界析出,铸坯在矫直过程形成裂纹,进而在轧制过程形成线材表面结疤。取样分析证实,精炼过程使用高N含量(4.6%)缓释脱氧剂造渣是钢水含N高的主要原因;使用铝粒替代缓释脱氧剂脱氧造渣,精炼过程增N 量可由43.4 x 10
-6
降至11.4 x 10
-6
通过将转炉出钢C由0.06%提高至30.08%、降低精炼前期加热功率、铝粒替代缓释脱氧剂造渣等措施
10B28钢N含量稳定控制在70 x 10
-6
以下,线材合格率由不足50%提升至≥98%。
Abstract
Through the analysis it is obtained that main reason for steel 10B28 scab is that nitrogen content in the molten steel is too high
and titanium in molten steel is not enough to completely fix nitrogen
resulting in a large number of fine BN precipitates at grain boundary
and the slab cracks are formed in the straightening process to form the wire surface scab in rolling process. Through sampling analysis
it is confirmed that the main cause of high nitrogen content in molten steel is slagging to use high nitrogen content (4.6% ) slow-release deoxidizer during refining. By using aluminum shot to replace slow-release deoxidizer
the nitrogen increases in refining process can be reduced from 43. 4 x 10
-6
to 11.4 x 10
-6
. By the measures including increasing the BOF tapping carbon from 0.06% to ≥ 0.08%
reducing the heating power in the early stage of refini
ng
and replace slow-release deoxidizer by Al shot
the nitrogen content of steel 10B28 is stably controlled below 70 x 10
-6
and the qualified rate of wire rod is increased from less than 50% to ≥ 98%.