ISSN:1003-8620

CN:42-1243/TF

主管:中信泰富特钢集团股份有限公司

主办:大冶特殊钢有限公司

特殊钢 ›› 2021, Vol. 42 ›› Issue (3): 27-30.

• 工艺技术 • 上一篇    下一篇

260 t转炉-RH流程IF钢DC06顶渣改质剂优化生产实践

胡巍1, 徐斌1, 黄嘉琦1, 朱文睿1,黎季1,李任春2,刘俊山2, 成日金1,3   

  1. 1. 武汉科技大学省部共建耐火材料与冶金国家重点实验室
    2. 河北钢铁集团邯钢分公司邯宝炼钢厂
    3. 河北钢铁集团邯钢分公司技术中心
  • 收稿日期:2020-11-02 出版日期:2021-05-15 发布日期:2022-11-11
  • 作者简介:胡巍(1998-),男,2020年武汉科技大学(本科)毕业,钢铁冶金研究。
  • 基金资助:
    武汉科技大学大学生创新创业训练计划项目 (18ZRA007),耐火材料与冶金国家重点实验室开放 基金(2018QN03)资助

Optimization and Production Practice of Top Slag Modifier for IF Steel DC06 with 260 t BOF-RH Flowsheet

Hu Wei1, Xu Bin1, Huang Jiaqi1, Zhu Wenrui1, Li Ji1, Li Renchun2, Liu Junshan2, Cheng Rijin1,3 #br#   

  1. 1 The State Key Laboratory of Refractories and Metallurgy, Wuhan University of Science and Technology, Wuhan 430081;
    2 Hanbao Steel making Plant, HBIS Group Hansteel Company, Handan 056001;
    3 Technical Center, HBIS Group Hansteel Company, Handan 056001
  • Received:2020-11-02 Published:2021-05-15 Online:2022-11-11

摘要: 为保证精炼渣有较好的脱氧与吸附夹杂物的能力,采取5种顶渣改质剂对无间隙原子钢(IF钢)转炉出钢钢包顶渣进行改质工业试验。并采用电感耦合等离子体原子发射光谱法(ICP-AES)对渣成分进行检测,运用FactSage软件对精炼渣粘度进行计算。研究结果表明,5种改质剂改质后,真空循环脱气(RH)出站时,5炉精炼渣中TFe含量控制在6.46%~7.76%,钙铝比(CaO)/(Al2O3)控制在1.60~1.86,1 600 ℃时精炼渣粘度在0.057~0.068 Pa·s,导致夹杂降级比为 2.10%~12.86%,3号改质剂(48.5% Al-10.2% Al2O3-18.1%CaO-6.0%SiO2-8.0% CaF2)综合性能最合适。采取转炉出钢碳由改进前的0.032%增大至0.045%,优化改质剂用于生产后,RH进站精炼渣中全铁(TFe)控制在7.13%,RH出站渣中FeO控制在5.52%,热轧时因顶渣改质造成的废次比为0.071%,降低了20.2%。 

关键词: IF超低碳钢DC06, RH, 改质剂, 精炼渣, 全铁, 废次比

Abstract: In order to ensure that the refining slag has better deoxidation and absorption ability of inclusions, the five top slag modifiers are used to carry out industrial tests on the top slag of the converter tapping ladle of IF steel. ICP-AES (Induction Coupling Plasma-Atomic Emission Spectroscopy) is used to detect the slag composition and FactSage software is used to calculate the viscosity of refining slag. The results show the vacuum circulation degassing (RH) is out the station, after 5 kinds of madifiers are used, that the content of TFe in the refining slag of 5 heats is controlled at 6. 46% ~7. 76%, the ( CaO)/(Al2O3) ratio is 1. 60 ~ 1. 86 at 1 600 ℃, the viscosity of refining slag is 0. 057 ~ 0. 068 Pa ·s, the degradation ratio of degradation caused by inclusions is 2. 10% ~ 12. 86%, and No. 3 modifier (48. 5% Al-10. 2% Al2O3-18. 1% CaO-6. 0% SiO2-8- 0% CaF2) has the best comprehensive performance. After the carbon content in the steel increases to 0. 045% from 0. 032% during converter tapping, and the optimized modifier is used in production, the TFe content in slag before RH is controlled at 7. 13% , and the FeO content in slag after RH is controlled at 5. 52% and during hot rolling, the ratio of off-and sub-quality products with top slag modification is 0. 071%, which is reduced by 20. 2%.