Analysis and Optimization on Hot Metal KR Desulphurization Process by Response Surface Methodology
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Analysis and Optimization on Hot Metal KR Desulphurization Process by Response Surface Methodology
Special SteelVol. 36, Issue 3, Pages: 5-8(2015)
作者机构:
1. 大冶特殊钢股份有限公司炼钢事业部,黄石,435001
2. 高品质特殊钢湖北省重点实验室,黄石,435001
作者简介:
基金信息:
DOI:
CLC:
Received:03 December 2014,
Online First:17 August 2022,
Published:17 August 2015
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王震, 苏春阳, 潘明旭, et al. Analysis and Optimization on Hot Metal KR Desulphurization Process by Response Surface Methodology[J]. Special Steel, 2015, 36(3): 5-8.
DOI:
王震, 苏春阳, 潘明旭, et al. Analysis and Optimization on Hot Metal KR Desulphurization Process by Response Surface Methodology[J]. Special Steel, 2015, 36(3): 5-8.DOI:
Analysis and Optimization on Hot Metal KR Desulphurization Process by Response Surface Methodology
The effect of parameters including adding amount (650 〜950 kg) of desulfiirizer (/% : 80. 55CaO
0. 04S
0. 01P
4. 34SiO
2
6. 06CaF
2
0. 05H
2
O)
stirring time (7 ~ 11 min)
stirring impeller rotating speed (90 〜110 r/min) and submerged depth of impeller (850 ~ 1 150 mm) on efficiency of KR desulphurization of 115 ~ 117 t hot metal (0. 03% ~ 0. 06% S
1 250 〜1 350 ℃ ) has been statistic-analyzed and studied by using response surface method ( RSM)
and a equation of regression model is obtained. Results show that with using the optimized parameters- adding amount of desulfurizer 820 kg
stirring for 9 min
rotating speed of stirring impeller 101 r/min and submerged depth of impeller in bath 985 mm
with hot me
tal KR desulphurization the predicted value of efficiency of desulphurization is 91. 99%
while the real measured value is 90. 18%
the relative error is 2. 0% ; with optimized desulphurization process the consumption of used desulfurizer decreases and the first qualified rate of metal increases from original 88. 35% to 95. 88%.