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洛阳双瑞特种装备有限公司,洛阳,471000
Online First:13 July 2022,
Published:13 July 2017
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陈帅超, 王新鹏, 宁天信, et al. Commercial Pilot Production of Incoloy825 Alloy ESR 280mmx325mm Withdrawing Bloom[J]. Special Steel, 2017, 38(6): 49-52.
DOI:
陈帅超, 王新鹏, 宁天信, et al. Commercial Pilot Production of Incoloy825 Alloy ESR 280mmx325mm Withdrawing Bloom[J]. Special Steel, 2017, 38(6): 49-52. DOI:
试验了Incoloy825合金电极(/%:0.01C
0.21Si
0.41Mn
0.007S
0.019P
22.33Cr
39.08Ni
3.04Mo
2.14Cu
1.17Ti
0.17Al)由3t中频炉+3tAOD冶炼
并经抽锭电渣重熔成280mm×325 mm坯(/%:0.01C
0.21~0.23Si
0.40Mn
0.005S
0.023~0.024P
22.48~22.50Cr,39.10~39.13Ni
3.05~3.07Mo
2.14~2.15Cu
1.00~1.10Ti
0.15~0.18Al)。试验表明
Incoloy825合金方坯抽锭电渣重熔过程中
由于Ti烧损
渣中TiO
2
含量不断增加
熔渣的粘度也不断上升
导致钢渣不易分离。通过改进抽锭电渣重熔渣系配比
采用(/%)57CaF
2,
15CaO,5MgO
15Al
O
3
5SiO
3TiO
渣系以及控制电极熔化速度680kg/h
重熔过程加0.43kg/t铝粒以控制Ti烧损
使Incoloy825合金铸坯表面质量明显改善。
The electrodes of tested Incoloy825 alloy (/%: 0.01C
0. 21Si
0.17Al) are melted by 3t medium frequency induction furnace + 3t AOD
and the 280mmx325mm withdrawing blooms (/%: 0.01C
22.48~22.50Cr
39.10~39.13Ni
1.00~ 1.10Ti
0.15~0.18Al) are remelted by ESR process. The test results show that during ESR bloom withdrawing process of Incoloy825 alloy
due to Ti burning loss the TiO
content in slag increases continuously and the viscosity of slag also uninterrupted increases led to difficult separation of sl
ag and steel. By improving ingredient of slag for withdrawing bloom ESR
using (/%) 57CaF
15CaO
5MgO
slag series and controlling electrode melting rate 680kg/h and adding aluminium shot 0.43 kg/t in ESR process to control Ti burning loss
the surface quality of casting bloom of Incoloy825 alloy improves obviously.
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