Process Practice to Increase Qualified Rate of Internal-Controlled End-Quenched Hardenability of Gear Steel 8620RH(K)
|更新时间:2026-01-21
|
Process Practice to Increase Qualified Rate of Internal-Controlled End-Quenched Hardenability of Gear Steel 8620RH(K)
Special SteelVol. 39, Issue 5, Pages: 28-31(2018)
作者机构:
1. 华北理工大学迁安学院,迁安,064400
2. 河北钢铁集团石钢公司,石家庄,050000
作者简介:
基金信息:
DOI:
CLC:
Received:23 April 2018,
Online First:27 May 2022,
Published:27 May 2018
稿件说明:
移动端阅览
高菊, 丁志军, 李辉. Process Practice to Increase Qualified Rate of Internal-Controlled End-Quenched Hardenability of Gear Steel 8620RH(K)[J]. Special Steel, 2018, 39(5): 28-31.
DOI:
高菊, 丁志军, 李辉. Process Practice to Increase Qualified Rate of Internal-Controlled End-Quenched Hardenability of Gear Steel 8620RH(K)[J]. Special Steel, 2018, 39(5): 28-31.DOI:
Process Practice to Increase Qualified Rate of Internal-Controlled End-Quenched Hardenability of Gear Steel 8620RH(K)
The steelmaking flowsheet of gear steel 8620RH ( K) (/% : 0.18 ~0.22C
0. 17 ~0. 26Si
0.70 ~ 0. 90Mn
≤0.025P
0.015 ~ 0.025S
0.4 ~0.6Cr
0.4 ~0.7Ni
0.15 ~0.25Mo
0.015 ~ 0.045A1
≤0.0100N) is 60 t BOF-LF-VD-300 mm x360 mm casting bloom. The BOF end residual elements and tapping amount of steel
alloying adding amount in refining process
adding N method in VD process and carbon segregation of casting bloom in original process have been analyzed
it is obtained that the main causes of hardenability band width AHRC 4 〜5 being on low side in end-quench test are BOF liquid tapping amount not stable
higher superheating temperature extent of liquid in tundish
lower qualified rate of internal controlled compound of liquid and higher casting bloom carbon segregation index. With using the process measures including stabilizing BOF charging and tapping amount
blowing nitrogen to increase nitrogen in liquid in LF
idle hot ladle adding covering plate
controlling tundish liquid supeiheating temperature 15 ~25 ℃.
and optimizing casting electromagnetic stirring parameters
the qualified rate of internal-controlled end-quenched hardenability of steel 8620RH(K) increases from original <60% to 82.93%.