Effect of 210 t RH Refining Parameters on Cleanliness of Steelmaking-Rolling IF Steel and Process Optimization
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Effect of 210 t RH Refining Parameters on Cleanliness of Steelmaking-Rolling IF Steel and Process Optimization
Special SteelVol. 39, Issue 3, Pages: 31-34(2018)
作者机构:
1. 湖南华菱集团涟源钢铁有限公司一炼轧厂,娄底,417009
2. 湖南工业大学冶金与材料工程学院,株洲,412007
作者简介:
基金信息:
DOI:
CLC:
Received:20 December 2017,
Online First:02 June 2022,
Published:02 June 2018
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邓必荣, 张波, 周剑丰, et al. Effect of 210 t RH Refining Parameters on Cleanliness of Steelmaking-Rolling IF Steel and Process Optimization[J]. Special Steel, 2018, 39(3): 31-34.
DOI:
邓必荣, 张波, 周剑丰, et al. Effect of 210 t RH Refining Parameters on Cleanliness of Steelmaking-Rolling IF Steel and Process Optimization[J]. Special Steel, 2018, 39(3): 31-34.DOI:
Effect of 210 t RH Refining Parameters on Cleanliness of Steelmaking-Rolling IF Steel and Process Optimization
Based on statistics of process data of IF steel (/% : ≤ 0.002 5C
≤ 0. 005Si
0. 01 ~0
12Mn
≤ 0. 020P
≤ 0. 010S
0. 02 ~0. 04Als
0. 03 ~0. 05Ti) in steelmaking process
the effect of oxygen content in liquid at Ar station and amount of adding aluminium in RH decarburization period on T[O
]
and the effect of alloys adding procedure
top slag modified treatment and shielding casting process on cleanliness of liquid are analyzed. Research results show that the measures including proper increasing the BOF end oxygen content in liquid and temperature of liquid
extending the interval time between Al and Fe-Ti addition
top slag modifying treating and shielding casting process are available to increase the cleanliness of liquid. It is obtain
ed by commercial production that with the average temperature of liquid at initial RH refining increasing by 2. 4 °C
controlling BOF tapping slag amount to decrease the thickness of top slag layer from original 。80 mm to 60 ~75 mm as a result during RH decarburization process the adding aluminium heats decreasing by original 36% to 3%
and with top slag modification to decrease the (FeO + MnO) from original 22% to 17% and increase the continuous-continuous casting heats from 8 heats to 10 heats