ISSN:1003-8620

CN:42-1243/TF

Governed by: CITIC Pacific Special Steel Group Co., LTD

Sponsored by: Daye Special Steel Co., LTD.

Special Steel ›› 2013, Vol. 34 ›› Issue (4): 36-39.

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Analysis on Cracking and Perforation Defects of Heavy Plate Rolled from Large-Scale Ingot and Optimization of Casting Process

Cao Jilin1, Mao Zhigang1 , Zhao Xiangzheng2   

  1. 1 Henan Province Industrial School, Zhengzhou 450Q02
    2 First Steelmaking Works, Wuyang Iron and Steel Co, Wugang 462500
  • Received:2013-02-16 Online:2013-08-01 Published:2022-09-11

大型钢锭轧板开裂和穿孔缺陷分析及浇铸工艺优化

曹季林1,毛志刚1,赵向政2   

  1. 1河南省工业学校,郑州450002;
    2舞阳钢铁公司第一炼钢厂,舞钢462500
  • 作者简介:曹季林( 1972-),男,讲师,1996年昆明理工大学毕业,钢铁冶炼研究。

Abstract: An analysis on cracking and perforation defects occurred in 230 ~ 400 mm plates rolled from 28 ~40 t ingot of low carbon steel S355JR and S355J2 (/% : 0. 17 ~0. 20C, 0. 30 ~0. 55Si, 1.40 - 1.60Mn, W0.020P, W0.015S, 0. 020 ~ 0. 040Al, 0. 020 ~0. 030Nb) is carried out. With the optimum process measures including increasing level of operation crews, controlling ingot body and hot top casting speed according to overheating extent of liquid, controlling refining end [O] ≤ 25 x 10-6 and aluminum content in steel 0. 020% 〜0. 040%, the ingot qualified ratio by nondestructive testing increases to 96. 8%.

摘要: 分析了S355JR和S355J2低碳钢(/%:0.17~0.20C、0.30~0.55Si、1.40~1.60Mn、≤0.020P、≤0.015S、0.020~0.040A1、0.020~0.030Nb)28~40 t钢锭轧成230~400 mm钢板出现的开裂和穿孔缺陷。通过提高浇钢工操作水平,根据钢水过热度控制本体浇铸和帽口浇铸时问;控制精炼终点[O]≤25×10-6以及钢中铝含量0.020%~0.040%等优化浇铸工艺措施使钢锭探伤合格率提高到96.8%。

关键词: 低碳钢, 28 ~40 t大型钢锭, 厚板, 轧板开裂, 穿孔缺陷, 工艺优化