叶凡新, 冯文甫, 郭志彬, 等. 60 t AOD全铁水精炼400系不锈钢热补偿技术的工艺实践[J]. 特殊钢, 2016,37(6):44-46.
叶凡新, 冯文甫, 郭志彬, et al. Process Practice of Thermal Compensation Technology for Refining 400 Series Stainless Steels in a 60 t AOD with Hot Metal[J]. Special Steel, 2016, 37(6): 44-46.
叶凡新, 冯文甫, 郭志彬, 等. 60 t AOD全铁水精炼400系不锈钢热补偿技术的工艺实践[J]. 特殊钢, 2016,37(6):44-46.DOI:
叶凡新, 冯文甫, 郭志彬, et al. Process Practice of Thermal Compensation Technology for Refining 400 Series Stainless Steels in a 60 t AOD with Hot Metal[J]. Special Steel, 2016, 37(6): 44-46.DOI:
严重制约着生产顺行和质量改善。通过工业实践研究了60 t AOD枪位(1.5~3.5 m)对CO二次燃烧比的影响
铬铁中硅含量(1%~6.5%)对石灰消耗和综合提供热量的影响
以及烘烤时间(0.5~4.5 h)对合金温度的影响。结果表明
60 t AOD氧枪枪位控制在3 m时CO二次燃烧的比例可提高至20%;铬铁中硅含量为4%时综合功效最大;合金最佳烘烤时间为2~3 h。
Abstract
During refining process of steel 1Cr13 etc 400 series stainless steels in a 60 t AOD unit with direct charging hot metal
due to adding large amount of materials including ferrochromium alloy
slag-forming addition and return scrap
the required heat accounts for 15% 〜40% of the total heat of bath
that seriously restricts smooth refining and improving liquid quality. The effect of 60 t AOD lance level (1.5 ~ 3. 5 m) on CO post-combustion ratio
the effect of silicon content (1 % ~6. 5%) in ferrochrome on lime consumption and comprehensive supply of heat and the effect o£ baking time (0. 5 ~ 4. 5 h) on alloy temperature are studied by commercial production practice. Results show that with controlling 60 t AOD oxygen lance level at 3 m the CO post-combustion ratio increases to 20% ; with 4% silicon content in ferrochrome the comprehensive work efficiency is maximum ; and the time of alloy baking for 2 ~ 3 h is optimum.