ISSN:1003-8620

CN:42-1243/TF

Governed by: CITIC Pacific Special Steel Group Co., LTD

Sponsored by: Daye Special Steel Co., LTD.

Special Steel ›› 2015, Vol. 36 ›› Issue (6): 16-19.

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Practice of Cold Drawing Process Optimization of GCr15 Bearing Steel Rod

Wang Yingying ,Yang Pengyuan   

  1. Dalian Special Steel Co Ltd, Dongbei Special Steel Group, Dalian 116105
  • Received:2015-06-02 Online:2015-12-01 Published:2022-08-12

GCr15轴承钢线材冷拔工艺优化的实践

王莹莹,杨鹏远   

  1. 东北特钢集团大连特殊钢有限责任公司,大连116105
  • 作者简介:王莹莹(1983-),女,工程师,2006年辽宁科技大学(本科) 毕业,金属材料及热处理研究。

Abstract: The effect of draft, cone angle and length of sizing belt of drawing die, and drawing speed on drawing stress and drawing surface accuracy of bearing steel GCr15 (1. 01% C, 1. 58% Cr) Φ11 mm rod coil has been analyzed. The optimization process for Φ11 mm rod coil cold drawing to Φ10. 2 mm rod is obtained, i. e. Φ11 mm rod coil (HB193)- isothermal spheroidizing annealing (at 785℃ for 4. 5 h → at 750 °C for 3 h) - cold drawing to 10. 4 mm rodde-stress annealing at 740 ℃ for 4. 5 h- cold drawing to Φ10. 2 mm rod products (HB205) ; the nice surface quality is obtained by using the process measures including with cold speed 35 m/min and drawing oil lubricant.

摘要: 分析了GCr15轴承钢(1.01%C,1.58%Cr)Φ11 mm线材的减面率、拉拔模角度和定径带长度,拉拔速率对拉拔应力和拉拔表面精度的影响。得出Φ11 mm盘条冷拉至Φ10.2 mm线材的优化工艺,即Φ11 mm线材(HB193)-等温球化退火(785℃4.5 h→750℃3 h)-冷拔至中10.4 mm盘条-740℃4.5 h去应力退火-冷拔至Φ10.2 mm棒材成品(HB205);冷拔速度35 m/min,油性润滑等工艺措施可获良好的表面质量。

关键词: GCr15轴承钢线材, 联合拉拔机, 冷拔, 减面率, 模具, 应力, 等温球化退火, 润滑