ISSN:1003-8620

CN:42-1243/TF

Governed by: CITIC Pacific Special Steel Group Co., LTD

Sponsored by: Daye Special Steel Co., LTD.

Special Steel ›› 2009, Vol. 30 ›› Issue (6): 42-44.

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Optimization of Bloom Casting Process for R3 Grade Offshore Mooring Chain Steel

Ji Kejin1 , Chen Jihong3, Chen Jun2, Wang Ping3, Liu Gaoli3   

  1. 1 Quality Examination Department;
    2 Technology Center;
    3 No4 Steelmaking Works, Daye Special Steel Corp Ltd, Huangshi 435001
  • Received:2009-06-26 Online:2009-12-01 Published:2022-11-29

R3级海洋系泊链用钢大方坯连铸工艺优化

季克进1,陈继红3,陈 君2,王 品3,刘高丽3   

  1. 大冶特殊钢股份有限公司,1质量检验部;
    2技术中心;
    3四炼钢厂,黄石435001
  • 作者简介:季克进(1961-),男,工程师,1983年本溪冶金专科学校毕业,钢材产品生产过程质量控制研究。

Abstract: With taking the technology measures such as increasing Mn content in steel from 1. 55% ~ 1.65% to 1,75% 〜1. 85% , replacing 0. 20% ~0. 25% Ni in steel by 0. 25% 〜0. 35% Cr, adding 0. 01 % ~0. 04% Ti for microalloying, controlling [ N] ≤80 x 10-6 and [O] ≤15 x 10-6 by RH vacuum treatment, decreasing casting secondary cooling water rate from 0. 11 L/kg to 0. 08 L/kg and modifying water distribution ratio to increase temperature of bloom at outlet from 620 ~ 680 ℃ to 700 ~ 750 °C , bloom cooling with shielding and bar products slow cooling, the production cost of R3 grade mooring chain steel is reduced, the longitudinal cracks of 350 mm x 470 mm cast bloom are eliminated and the strength and the toughness at -20 ℃ of products all meet the requirement of standard.

摘要: 通过将钢中Mn含量从1.55%~1.65%提高至1.75%~1.85%,用0.25%~0.35%Cr替代0.20%~0.25%Ni,并加入0.01%~0.04%Ti微合金化;RH真空精炼以控制[N]≤80×10-6、[O]≤15×10-6;连铸二冷水量由0.11 L/kg降至0.08 L/kg,并改变配水比例,使出坯温度由620~680℃提高至700~750℃,并采用连铸坯罩冷和钢材缓冷等工艺措施,降低了R3级系泊链钢的生产成本,避免了350 mm×470 mm铸坯纵裂的产生,并使钢材的强度和-20℃韧性均满足标准要求。

关键词: R3级海洋系泊链钢, 大方坯连铸, 工艺优化