002 0[0])的冶金流程为铁水脱硫预处理-120 t 转炉-LF-RH-280 nun x 380 mm 坯连铸。分析证实铸坯偏析是钢轨低倍检验和超声波探伤不合格的主要原因。试验研究了钢水过热度、拉速、结 晶器电磁搅拌、二冷水量和凝固末端动态轻压下对铸坯中心碳偏析的影响。通过采用优化的工艺措施:钢水过热 度15~30 拉速0.60 - 0. 75 m/min和恒拉速
The metallurgical flow sheet o£ studied heavy rail steel (/% : 0. 68 ~ 0. 73C
0. 20 ~ 0. 30Si
1. 05 ~ 1. 15Mn
≤0.015P
≤0.012S
≤O.OO3 5A1
≤0.000 15[H],≤0.006 0[N]
≤0.002 0 [0]) is metal desulphurization pretreated- 120 t converter-LF-RH-280 mm x 380 mm bloom easting. It is identified by analysis that the casting bloom segregation is main cause for unqualified rolled rail by macrostructure examination and supersonic testing. The effect of liquid overheating extend
casting speed
mould magnetic stirring
secondary water cooling rate and dynamic soft reduction at end of solidification on center carbon segregation of casting bloom is tested and studied. With using the optimized process measures including controlling liquid overheating extent 15 ~ 30 T
secondary water cooling rate 0. 25 L/kg and soft reduction 6 〜7 mm
the rating of general porosity ≤1. 0
of center porosity ≤0. 5
of spot segregation ≤0. 5
the ratio of equiaxed zone is more than 37%
the center carbon segregation index is 0. 94 ~ 1. 06 and the qualified ratio of steel rail tested by supersonic method increases up to more than 99. 3%.